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Treatment of Landfill Leachate Using A/O-Coagulation-BDD:Ⅰ. Parameter Optimization
Yingchun SHAN, Qingwei WANG, Weiyi PAN, Wanzi SHI, Haimei SUN, Weiling SUN
Acta Scientiarum Naturalium Universitatis Pekinensis    2017, 53 (3): 497-506.   DOI: 10.13209/j.0479-8023.20175.044
Abstract823)   HTML2)    PDF(pc) (949KB)(207)       Save

Landfill leachate was treated by A/O-coagulation-BDD combined processes, and the operation parameters were optimized. The optimal HRT and sludge recirculation ratio was 10.7 days and 3.5 for A/O treatment process. Reaction pH and optimal dose of ferric chloride coagulation treatment was 5.5 and 0.4 g/L. The current density and A/V ratio (anode area/reaction volum) for best performance of BDD was 60 mA/cm2 and 4 m-1. CODCr concentration in raw leachte and final effluent were 13375 mg/L and 60 mg/L, with the removal efficiency of 99.5%. TOC concentration before and after treatment by combined treatment process were 6893 mg/L and 12 mg/L, with the removal efficiency of 99.8%. Ammonia nitrogen was completely removed by the combined treatment processes from 1889 mg/L to 0 mg/L. The contribution of A/O, coagulation, and BDD was 59.0%, 32.9%, and 7.6% for CODCr removal of total CODCr, was 50.5%, 46.1%, and 13.2% for TOC removal, was 84.3%, 2.5%, and 3.2% for ammonia nitrogen removal, respectively.

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